![]() As you can see from the image above the process itself was a success!įrom here, the PCB design will go back to square one. This PCB came from a new manufacturing process where I used a laminator and gloss paper as the toner transfer method. Its important to stress that while this PCB hasn’t been a success, it hasn’t been a failure either. Physical component wise, the LED’s were situated too close to each other, meaning that when it came to solder them, they were all on-top of one another. The placement of the GPIO connector (13 x 2 lines of pins) meant that the board was in an awkward position and the cable pushed up against the accelerator / motion detector. Following what I thought to be a simple design I quickly found out that I had errors both in the pin layout and the physical spacing of the components used on the board.
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